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Update Scooter_2_servos.ino#1

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jjurski wants to merge 1 commit into
martintrowland:mainfrom
jjurski:patch-1
Open

Update Scooter_2_servos.ino#1
jjurski wants to merge 1 commit into
martintrowland:mainfrom
jjurski:patch-1

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@jjurski
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@jjurski jjurski commented Feb 11, 2023

There was a wrong value set for stopping the 360 motor

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@martintrowland martintrowland left a comment

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This is the issue with quality of the motors. My robot actually requires the value 89 to stop on his left motor...... Now that we have 5 robots I see the variation between servos and their battery power is quite significant. I also have realized that the 9V batteries don't have enough current to run these robots. I have a rechargable 9V which has 800mAH.... hmmmm

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